Wykres commitów

5 Commity (f7d6108d1ad83f26598e73d3b163f3de411c902b)

Autor SHA1 Wiadomość Data
stijn 42c4dd09a1 py/nlr: Fix missing trailing characters in comments in nlr.c 2017-12-29 22:24:53 +11:00
stijn b184b6ae53 py/nlr: Fix nlr functions for 64bit ports built with gcc on Windows
The number of registers used should be 10, not 12, to match the assembly
code in nlrx64.c. With this change the 64bit mingw builds don't need to
use the setjmp implementation, and this fixes miscellaneous crashes and
assertion failures as reported in #1751 for instance.

To avoid mistakes in the future where something gcc-related for Windows
only gets fixed for one particular compiler/environment combination,
make use of a MICROPY_NLR_OS_WINDOWS macro.

To make sure everything nlr-related is now ok when built with gcc this
has been verified with:
- unix port built with gcc on Cygwin (i686-pc-cygwin-gcc and
  x86_64-pc-cygwin-gcc, version 6.4.0)
- windows port built with mingw-w64's gcc from Cygwin
 (i686-w64-mingw32-gcc and x86_64-w64-mingw32-gcc, version 6.4.0)
 and MSYS2 (like the ones on Cygwin but version 7.2.0)
2017-12-29 22:24:46 +11:00
Damien George b25f92160b py/nlr: Factor out common NLR code to macro and generic funcs in nlr.c.
Each NLR implementation (Thumb, x86, x64, xtensa, setjmp) duplicates a lot
of the NLR code, specifically that dealing with pushing and popping the NLR
pointer to maintain the linked-list of NLR buffers.  This patch factors all
of that code out of the specific implementations into generic functions in
nlr.c, along with a helper macro in nlr.h.  This eliminates duplicated
code.
2017-12-28 16:46:30 +11:00
Paul Sokolovsky 096e967aad Revert "py/nlr: Factor out common NLR code to generic functions."
This reverts commit 6a3a742a6c.

The above commit has number of faults starting from the motivation down
to the actual implementation.

1. Faulty implementation.

The original code contained functions like:

NORETURN void nlr_jump(void *val) {
    nlr_buf_t **top_ptr = &MP_STATE_THREAD(nlr_top);
    nlr_buf_t *top = *top_ptr;
...
     __asm volatile (
    "mov    %0, %%edx           \n" // %edx points to nlr_buf
    "mov    28(%%edx), %%esi    \n" // load saved %esi
    "mov    24(%%edx), %%edi    \n" // load saved %edi
    "mov    20(%%edx), %%ebx    \n" // load saved %ebx
    "mov    16(%%edx), %%esp    \n" // load saved %esp
    "mov    12(%%edx), %%ebp    \n" // load saved %ebp
    "mov    8(%%edx), %%eax     \n" // load saved %eip
    "mov    %%eax, (%%esp)      \n" // store saved %eip to stack
    "xor    %%eax, %%eax        \n" // clear return register
    "inc    %%al                \n" // increase to make 1, non-local return
     "ret                        \n" // return
    :                               // output operands
    : "r"(top)                      // input operands
    :                               // clobbered registers
     );
}

Which clearly stated that C-level variable should be a parameter of the
assembly, whcih then moved it into correct register.

Whereas now it's:

NORETURN void nlr_jump_tail(nlr_buf_t *top) {
    (void)top;

    __asm volatile (
    "mov    28(%edx), %esi      \n" // load saved %esi
    "mov    24(%edx), %edi      \n" // load saved %edi
    "mov    20(%edx), %ebx      \n" // load saved %ebx
    "mov    16(%edx), %esp      \n" // load saved %esp
    "mov    12(%edx), %ebp      \n" // load saved %ebp
    "mov    8(%edx), %eax       \n" // load saved %eip
    "mov    %eax, (%esp)        \n" // store saved %eip to stack
    "xor    %eax, %eax          \n" // clear return register
    "inc    %al                 \n" // increase to make 1, non-local return
    "ret                        \n" // return
    );

    for (;;); // needed to silence compiler warning
}

Which just tries to perform operations on a completely random register (edx
in this case). The outcome is the expected: saving the pure random luck of
the compiler putting the right value in the random register above, there's
a crash.

2. Non-critical assessment.

The original commit message says "There is a small overhead introduced
(typically 1 machine instruction)". That machine instruction is a call
if a compiler doesn't perform tail optimization (happens regularly), and
it's 1 instruction only with the broken code shown above, fixing it
requires adding more. With inefficiencies already presented in the NLR
code, the overhead becomes "considerable" (several times more than 1%),
not "small".

The commit message also says "This eliminates duplicated code.". An
obvious way to eliminate duplication would be to factor out common code
to macros, not introduce overhead and breakage like above.

3. Faulty motivation.

All this started with a report of warnings/errors happening for a niche
compiler. It could have been solved in one the direct ways: a) fixing it
just for affected compiler(s); b) rewriting it in proper assembly (like
it was before BTW); c) by not doing anything at all, MICROPY_NLR_SETJMP
exists exactly to address minor-impact cases like thar (where a) or b) are
not applicable). Instead, a backwards "solution" was put forward, leading
to all the issues above.

The best action thus appears to be revert and rework, not trying to work
around what went haywire in the first place.
2017-12-26 19:27:58 +02:00
Damien George 6a3a742a6c py/nlr: Factor out common NLR code to generic functions.
Each NLR implementation (Thumb, x86, x64, xtensa, setjmp) duplicates a lot
of the NLR code, specifically that dealing with pushing and popping the NLR
pointer to maintain the linked-list of NLR buffers.  This patch factors all
of that code out of the specific implementations into generic functions in
nlr.c.  This eliminates duplicated code.

The factoring also allows to make the machine-specific NLR code pure
assembler code, thus allowing nlrthumb.c to use naked function attributes
in the correct way (naked functions can only have basic inline assembler
code in them).

There is a small overhead introduced (typically 1 machine instruction)
because now the generic nlr_jump() must call nlr_jump_tail() rather than
them being one combined function.
2017-12-20 15:42:06 +11:00